Posted
Michigan today released a report stating that loose bolts broke on the Chaos ride at Michigan's Adventure, causing the ride to come down. Cedar Fair has confirmed that the ride will not be brought back.
Read more from the Muskegon Chronicle.
Sorry, had to say it. I credit Dan with the joke.
-----------------
Jeff - Webmaster/Admin - CoasterBuzz.com, Sillynonsense.com
"As far as I can tell it doesn't matter who you are. If you can believe, there's something worth fighting for..." - Garbage, "Parade"
-------------
Kara
403 Laps
Prediction: Cedar Fair is going to blame maintenance procedures that were already in place when they bought the park, procedures which do not reflect procedures at other Cedar Fair parks, or currently in place at Michigan's Adventure. In other words, they won't deny responsibility for the incident, but they will note that it could never have happened in their other parks.
--Dave Althoff, Jr.
-----------------
This will be my 8th year at Valleyfair, can I go for 10? I know 2003 will be our turn!
-Ride_Op
-----------------
NoLimits Tournament of Champions now underway at Ride_Op Coaster Productions! http://rideop.twistedrails.com
-----------------
Jeff - Webmaster/Admin - CoasterBuzz.com, Sillynonsense.com
"As far as I can tell it doesn't matter who you are. If you can believe, there's something worth fighting for..." - Garbage, "Parade"
-----------------
It's conflict that shows who a person really is!
The findings of the report were hardly a surprise. On Monday, July 30, the ride came apart, and on Friday, August 3, Chance issued a new bulletin (B408R1181-B)...but the information in the new bulletin was the same as the information in an older bulletin (B408R1181-A). What does it say? It says, "Using a torque wrench, check for proper torque of all 28 capscrews. Torque value for checking these capscrews must be 80 ft-lbs. IMPORTANT: ALL 28 CAPSCREWS MUST BE TIGHTENED AND MAINTAINED AS DESCRIBED TO OPERATE THE RIDE."
Michigan apparently asked, but Michigan's Adventure was not able or not willing to document that the torque had been checked. If it's not documented, then as far as the state is concerned, it never happened. Particularly since there is evidence (I'm guessing 56 half-bolts...) that the ride had loose bolts.
Now let's consider one other possible scenario. Remember, most of us don't work for Michigan's Adventure, and I don't think any of us worked on their Chaos. But according to the bulletin, it is likely that the Chaos in question used two different length bolts...some 1-3/4" long, some 2-1/4" long. It's entirely possible that one or more of the 2-1/4" bolts got installed into 1-3/4" deep holes, in which case, if the hole is almost but not quite deep enough for the longer bolt, that the bolt could be at 80 ft-lbs but still not tight. If that is the case, they could quite easily have checked the bolt torque monthly and still had a problem because of an installation error. Doubtful because I think 90 ft-lbs (the installation torque) might be enough in that case to snap the heads off, but certainly possible.
--Dave Althoff, Jr.
You must be logged in to post